Ultra Seal® Well Bond – VR24 Wells

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Well Information

VR24 Well #8:

Client wanted to test the 11” 15m casing void to 5,000psi.

Service Tech. could only build 200psi on void while running test pump at full capacity. Service Tech. squeezed a total of 2 liters of Well Bond into the void.
Void tested to 5,000 psi.

 

VR24 Well #8:

Client wanted to test the 16 ¾” 3m casing void to 3,000psi.

Service Tech pressured the void to 3,000 psi., and it bled down to 1,900 psi. within 5 mins. Service Tech squeezed a total of 1 liter of Well Bond into the void.
Voided tested to 3,000 psi.

 

VR24 Well #10:

Client wanted to test the 9” 15m tubing hanger void to 5,000psi.

Service Tech pressured up to 5,000 psi., and it bled down to 500 psi within 15 mins. Service Tech squeezed a total of 1 liter of Well Bond into the void.
Void tested to 5,000 psi

Three days later the client pulled the tree and tested the BOPs against the hanger to 5,000 psi without failure.